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苑鹏等:超低碳钢顶渣氧化性对钢液洁净度的影响 *1709· 成Als]和T]的损失值增大,由此生成较多的A山0 and numerical simulation of flow field in slab casting mold with 夹杂物和A山,0,-T,0夹杂物,因此氧化性顶渣对洁净 different width.Spec Steel,2010,31 (1):14 (张大江,陈登福,王翠娜,等.不同宽度板坯结品器内流场 度的危害会持续至浇注结束.根据图22所示结果,应 的水模型和数值模拟研究.特殊钢,2010,31(1):14) 进一步采取措施,继续降低RH结束渣T.Fe含量. Ramos I C,Morales R D,Garcia-Hernandez S,et al.Effects of 2[AI]+3[0]=(AL,03), (1) immersion depth on flow turbulence of liquid steel in a slab mold 4[0]+xTi]+2[l]=(AL,0,-Ti,0).(2) using a nozzle with upward angle rectangular ports.IS/J Int, 2014,54(8):1797 3结论 8]Wu D F.Cheng SS.Effect of Sen design on surface fluctuation (1)通过对顶渣改质,顶渣中T.Fe的质量分数由 and solidifying shell in slab mold and its optimization.Acta Metall Sin Engl Lett,2008,21(5):341 转炉终点的19.18%降至RH进站时的4.68%,顶渣 9]Furumai K,Matsui Y,Murai T,et al.Evaluation of defect distri- 氧化性降低明显 bution in continuously-cast slabs by using ultrasonic defect detec- (2)转炉出钢至RH进站过程,钢中[O]的降低 tion system and effect of electromagnetic brake on decreasing un- 与顶渣T.Fe降低呈线性关系.RH进站渣T.Fe较低 balanced flow in mold./S//Int,2015,55(10):2135 的炉次,对应钢中[O]较低,吹氧炉次和RH深脱碳过 [0]Kittaka S,Watanabe K,Kanki T,et al.Nippon steel in-mold 程的平均吹氧量均较多,导致这些炉次铝脱氧前的 electro-magnetic stirrer "M-EMS"for slab caster.Nippon Steel [O]较高. Tech Rep,2002,86:68 [11]Yue F,Cui H,Li P H,et al.Study on the optimum process of (3)除少数炉次外,RH真空处理结束后钢中夹 refining ULC steel by RH degasser.J Univ Sci Technol Beijing, 杂物的数量与结束渣T.Fe呈线性关系,铝脱氧前钢中 2009,30(Suppl1):53 [O]与RH结束后钢中夹杂物的数量无明显关系 (岳蜂,崔衡,李朋欢,等.RH冶炼超低碳钢的最优工艺研 (4)RH进站渣(CaO)/(AL,O3)质量比过高或过 究.北京科技大学学报,2009,31(增刊1):53) 低都会影响AL03夹杂物被顶渣的吸收,导致这些炉 [12]Ou H L,Bao Y P,Yue F,et al.A study of water modeling on 次夹杂物数量较多 circulation flow rate in RH vacuum refining process.Spec Steel, 2011,32(3):9 (5)镇静和浇注过程氧化性顶渣会持续危害钢液 (欧洪林,包蒸平,岳蜂,等.H真空精炼过程循环流量的 洁净度,导致钢液[Als]和T]的损失值增大 水模型研究.特殊钢,2011,32(3):9) (6)顶渣氧化性影响钢液洁净度,进而影响浸入 [13]Cui H,Chen B,Wang M.et al.Cleanliness control of IF steel 式水口出口的堵塞.因此,顶渣氧化性较低的炉次,对 during the RH refining process.Unie Sci Technol Beijing, 应的热轧板卷缺陷率较低 2011,32(Suppl1):147 (崔衡,陈斌,王敏,等.RH精炼过程中F钢洁净度控制 参考文献 北京科技大学学报,2011,33(增刊1):147) [Hanao M,Kawamoto M.Influence of mold flux basicity on surface [14]Cui H,Tian E H,Chen B,et al.Cleanliness study of IF steel quality of ultra-ow carbon steel slabs.IS/Int,2008,48 (9): by holding in ladles after RH vacuum process.J Unir Sci Technol 1210 Beijing,2014,35(Suppl1):32) Li M Y,Zhang H B,Yang J,et al.Analysis and control of hot- (崔衡,田恩华,陈斌,等.RH真空精炼后F钢镇静工艺的 rolled coil surface inclusions of low carbon low silicon aluminium 洁净度研究.北京科技大学学报,2014,36(增刊1):32) killed steel.Steelmaking,2014,30(6):28 05] Zhang J J,Gao W F,Cao T Y,et al.Research on optimization (李梦英,张洪波,杨杰,等.低碳铝镇静钢热轧板表面夹渣 of flow field in WISCO 60 t two-strand tundish.Steelmaking, 的原因分析与控制.炼钢,2014,30(6):28) 2013,29(5):61 B]Wang X H.Non-metallic inclusion control technology for high (张剑君,高文芳,曹同友,等.武钢601双流连铸中间包流 quality cold rolled steel sheets.Iron Steel,2013,48(9):1 场优化试验研究.炼钢,2013,29(5):61) (王新华.高品质冷轧薄板钢中非金属夹杂物控制技术.钢 [16]Yuan P,Deng XX,Jiang M,et al.Investigation of subsurface 铁,2013,48(9):1) hooks in continuous cast low carbon aluminum-killed steel slab. 4]Chen D F,Zhang X G,Zhang L F,et al.Simulation on the be- Iron Steel,2015,50(8):24 havior of argon bubbles in slab continuous casting mold.Iron (苑鹏,邓小旋,姜敏,等.低碳铝镇静钢铸坯皮下钩状坯 Seel,2010,45(4):20 壳.钢铁,2015,50(8):24) (陈登福,张献光,张立峰,等.板坯连铸结晶器内氩气泡行 [17]Yuan P,Wang X H,Jiang M,et al.Inclusions in low carbon 为的模拟研究.钢铁,2010,45(4):20) aluminum killed steel slabs at high casting speed.Chin/Eng, [5]Liu Z Q.Qi FS,Li B K,et al.Vortex flow pattern in a slab con- 2016,38(3):342 tinuous casting mold with argon gas injection.ron Steel Res Int, (苑鹏,王新华,姜敏,等。高拉速连铸低碳铝镇静钢铸坯中 2014,21(12):1081 夹杂物.工程科学学报,2016,38(3):342) [6]Zhang D J,Chen D F,Wang C N,et al.A study on water model [18]Tsukaguchi Y,Hayashi H,Kurimoto H,et al.Development of苑 鹏等: 超低碳钢顶渣氧化性对钢液洁净度的影响 成[Als]和[Ti]的损失值增大,由此生成较多的 Al2O3 夹杂物和 Al2O3 --TixO 夹杂物,因此氧化性顶渣对洁净 度的危害会持续至浇注结束. 根据图 22 所示结果,应 进一步采取措施,继续降低 RH 结束渣 T. Fe 含量. 2[Al]+ 3[O]= ( Al2O3 ) , ( 1) 4[O]+ x[Ti]+ 2[Al]= ( Al2O3--TixO) . ( 2) 3 结论 ( 1) 通过对顶渣改质,顶渣中 T. Fe 的质量分数由 转炉终点的 19. 18% 降至 RH 进站时的 4. 68% ,顶渣 氧化性降低明显. ( 2) 转炉出钢至 RH 进站过程,钢中[O]的降低 与顶渣 T. Fe 降低呈线性关系. RH 进站渣 T. Fe 较低 的炉次,对应钢中[O]较低,吹氧炉次和 RH 深脱碳过 程的平均吹氧量均较多,导致这些炉次铝脱氧前的 [O]较高. ( 3) 除少数炉次外,RH 真空处理结束后钢中夹 杂物的数量与结束渣 T. Fe 呈线性关系,铝脱氧前钢中 [O]与 RH 结束后钢中夹杂物的数量无明显关系. ( 4) RH 进站渣( CaO) /( Al2O3 ) 质量比过高或过 低都会影响 Al2O3 夹杂物被顶渣的吸收,导致这些炉 次夹杂物数量较多. ( 5) 镇静和浇注过程氧化性顶渣会持续危害钢液 洁净度,导致钢液[Als]和[Ti]的损失值增大. ( 6) 顶渣氧化性影响钢液洁净度,进而影响浸入 式水口出口的堵塞. 因此,顶渣氧化性较低的炉次,对 应的热轧板卷缺陷率较低. 参 考 文 献 [1] Hanao M,Kawamoto M. Influence of mold flux basicity on surface quality of ultra-low carbon steel slabs. ISIJ Int,2008,48 ( 9 ) : 1210 [2] Li M Y,Zhang H B,Yang J,et al. Analysis and control of hot￾rolled coil surface inclusions of low carbon low silicon aluminium killed steel. Steelmaking,2014,30( 6) : 28 ( 李梦英,张洪波,杨杰,等. 低碳铝镇静钢热轧板表面夹渣 的原因分析与控制. 炼钢,2014,30( 6) : 28) [3] Wang X H. Non-metallic inclusion control technology for high quality cold rolled steel sheets. Iron Steel,2013,48( 9) : 1 ( 王新华. 高品质冷轧薄板钢中非金属夹杂物控制技术. 钢 铁,2013,48( 9) : 1) [4] Chen D F,Zhang X G,Zhang L F,et al. Simulation on the be￾havior of argon bubbles in slab continuous casting mold. Iron Steel,2010,45( 4) : 20 ( 陈登福,张献光,张立峰,等. 板坯连铸结晶器内氩气泡行 为的模拟研究. 钢铁,2010,45( 4) : 20) [5] Liu Z Q,Qi F S,Li B K,et al. Vortex flow pattern in a slab con￾tinuous casting mold with argon gas injection. J Iron Steel Res Int, 2014,21( 12) : 1081 [6] Zhang D J,Chen D F,Wang C N,et al. A study on water model and numerical simulation of flow field in slab casting mold with different width. Spec Steel,2010,31( 1) : 14 ( 张大江,陈登福,王翠娜,等. 不同宽度板坯结晶器内流场 的水模型和数值模拟研究. 特殊钢,2010,31( 1) : 14) [7] Ramos I C,Morales R D,Garcia-Hernandez S,et al. Effects of immersion depth on flow turbulence of liquid steel in a slab mold using a nozzle with upward angle rectangular ports. ISIJ Int, 2014,54( 8) : 1797 [8] Wu D F,Cheng S S. Effect of Sen design on surface fluctuation and solidifying shell in slab mold and its optimization. Acta Metall Sin Engl Lett,2008,21( 5) : 341 [9] Furumai K,Matsui Y,Murai T,et al. Evaluation of defect distri￾bution in continuously-cast slabs by using ultrasonic defect detec￾tion system and effect of electromagnetic brake on decreasing un￾balanced flow in mold. ISIJ Int,2015,55( 10) : 2135 [10] Kittaka S,Watanabe K,Kanki T,et al. Nippon steel in-mold electro-magnetic stirrer“M--EMS”for slab caster. Nippon Steel Tech Rep,2002,86: 68 [11] Yue F,Cui H,Li P H,et al. Study on the optimum process of refining ULC steel by RH degasser. J Univ Sci Technol Beijing, 2009,30( Suppl 1) : 53 ( 岳峰,崔衡,李朋欢,等. RH 冶炼超低碳钢的最优工艺研 究. 北京科技大学学报,2009,31( 增刊 1) : 53) [12] Ou H L,Bao Y P,Yue F,et al. A study of water modeling on circulation flow rate in RH vacuum refining process. Spec Steel, 2011,32( 3) : 9 ( 欧洪林,包燕平,岳峰,等. RH 真空精炼过程循环流量的 水模型研究. 特殊钢,2011,32( 3) : 9) [13] Cui H,Chen B,Wang M,et al. Cleanliness control of IF steel during the RH refining process. J Univ Sci Technol Beijing, 2011,32( Suppl 1) : 147 ( 崔衡,陈斌,王敏,等. RH 精炼过程中 IF 钢洁净度控制. 北京科技大学学报,2011,33( 增刊 1) : 147) [14] Cui H,Tian E H,Chen B,et al. Cleanliness study of IF steel by holding in ladles after RH vacuum process. J Univ Sci Technol Beijing,2014,35( Suppl 1) : 32) ( 崔衡,田恩华,陈斌,等. RH 真空精炼后 IF 钢镇静工艺的 洁净度研究. 北京科技大学学报,2014,36( 增刊 1) : 32) [15] Zhang J J,Gao W F,Cao T Y,et al. Research on optimization of flow field in WISCO 60 t two-strand tundish. Steelmaking, 2013,29( 5) : 61 ( 张剑君,高文芳,曹同友,等. 武钢 60 t 双流连铸中间包流 场优化试验研究. 炼钢,2013,29( 5) : 61) [16] Yuan P,Deng X X,Jiang M,et al. Investigation of subsurface hooks in continuous cast low carbon aluminum-killed steel slab. Iron Steel,2015,50( 8) : 24 ( 苑鹏,邓小旋,姜敏,等. 低碳铝镇静钢铸坯皮下钩状坯 壳. 钢铁,2015,50( 8) : 24) [17] Yuan P,Wang X H,Jiang M,et al. Inclusions in low carbon aluminum killed steel slabs at high casting speed. Chin J Eng, 2016,38( 3) : 342 ( 苑鹏,王新华,姜敏,等. 高拉速连铸低碳铝镇静钢铸坯中 夹杂物. 工程科学学报,2016,38( 3) : 342) [18] Tsukaguchi Y,Hayashi H,Kurimoto H,et al. Development of ·1709·
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